My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
City Council Agenda and Packet 1979 06 05
PORTAL
>
CITY COUNCIL RECORDS
>
AGENDAS & PACKETS (45.010)
>
1973-1989 City Council Agendas and Packets
>
1979 City Council Agendas and Packets
>
City Council Agenda and Packet 1979 06 05
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
3/11/2021 1:30:40 PM
Creation date
12/29/2009 10:47:41 AM
Metadata
Fields
Template:
City Council Records
Doc Type
City Council Packet
Signed Date
6/5/1979
Supplemental fields
Test
CCAGPKT 1979 06 05
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
128
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
Show annotations
View images
View plain text
• <br /> • <br /> • - <br /> Mr. Josh Richardson • <br /> City of Lcuisvllle <br /> Page 2 <br /> 2. Lowering of 8" Water Main at Station 10+10 Rex Street. <br /> Based on grist information we received from the City, <br /> for design purposes, this was a 4 Water Main at this <br /> location. Consequently we had to lower the main which <br /> increased the trench length for lowering purposes. Refer <br /> to cost per C. 0. S 1, Part II. Additional costs as follows: <br /> a. Pavement Removal , Item 4: <br /> (5' x 18') ■ 10 s. y. x $5.00 $ 50.00 <br /> b. Instructed Contractor to backfill trench with <br /> Class 6 base material for public traffic <br /> convenience purposes. Trench depth and average <br /> 6 feet. Thus: <br /> (5'x17'x6' deep) = 34.5 tons x $45.00 - $ 1,552.00 <br /> c. H.B.A. Patching - Gr. 'E' , Item 18: <br /> (5'x18'x3" thick) = 1 .7 ton x $66.00 $ 112.00 <br /> d. Relocate Existing 8" Water Line, <br /> Bid Item No. 10 - 1 each s_1021,251 <br /> Part 2 Total (a+b;c+d) $ 2,714.00 <br /> 3. Lowering of 8" Water Main at Station 16+ 54 Rex Street. <br /> The storm sewer was designed with 0'3" of clearance <br /> between Storm Sewer 0. D. and 8" Water Main 0. D. . During <br /> construction the 8" Water Main was higher than anticipated <br /> by elevations taken at existing gate valves at the 8" water <br /> line. We could not raise the storm sewer due to minimum <br /> cover requirements of the storm sewer. Thusly we instructed <br /> the Contractor to lower the 6" Water line in this area. <br /> Additional costs are as follows: <br /> a. Pavement Removal , Item 4: <br /> (5'x28') - 15.5 s.y. x S5.00 * $ 77.00 <br /> b. Class 6 Base, Item 17: <br /> (51x28')6" depth) = 4.7 ton x $45.00 $ 211 .00 <br /> c. N.B.P. Patching - Gr. 'E' Item 18: <br /> (5'x28'x3" thick) = 2.6 ton x $66.00 $ 171 .00 <br /> d. Relocate Existing 8" :rater Line, <br /> Bid Item No. 10 - 1 each - - $ 1,000.00 <br /> Part 3 Total (a+b+c+d) - $ 1,459.00 <br />
The URL can be used to link to this page
Your browser does not support the video tag.